Bow Thruster Installation (2002)
Meridian, Sloop No. 139
Harmony, Sloop No. 38
Among the very few negatives of the 424 hull is its refusal to behave
itself in close quarter maneuvering under power. A look at the underbody
is all that’s needed to understand why the boat tracks so well
at sea, but maneuvers sluggishly under power in close quarters. The
smallish rudder is hung behind a large skeg; the propeller is located
relatively far forward, approximately under the bridge deck; and the
prop shaft is angled downward so that the prop wash mainly passes under
the rudder, minimizing prop torque but also virtually eliminating the
rudder “kick” that many boats can generate with a quick
burst of engine power against a hard-over rudder. When boat speed is
low, the high freeboard forward and the cutaway forefoot make the bow
react to currents and wind far more than to the frantic efforts of the
helmsman.
After thirteen years of docking trauma, and following consultation
with other owners who have installed bow thrusters (Many thanks to Don
Barber of Thisisit and Bill Dwyer of Overdraft), I decided
to treat Meridian to a mechanical crewman up forward. David Kimmel
of Harmony and I decided to do the project on both our boats
at the same time to gain whatever quantity discounts might be available,
and to help each other with the parts of the project that were to be
owner-accomplished. Planning and shopping, including a trip to the
Fort Lauderdale Boat Show, culminated in a decision to go with a Vetus
Model 5512 electric thruster with a nominal 6” diameter tunnel.
Design and Equipment Selection Considerations
Selection of the Vetus Model 5512 was driven by three factors:
- The size of the tunnel (6-inch diameter) allowed the unit to fit
in the narrow space aft of the forward water tank. Harmony
has aluminum tanks, and had a 12 ½” space there. Meridian
has fiberglass tanks and only 10 ½” of room. Selection of a
larger unit would have required that some of the cabinetry in the
vee-berth area be dismantled to accommodate the installation of the
tunnel tube, adding to the cost and complexity of the project.
- The shape of the hull in that area meant that the 30-inch long (standard)
tunnel would get the job done, albeit just barely. A longer tunnel
would not only have added significant cost to the project, but would
have compromised the thruster’s performance owing to tunnel
drag.
- The Vetus units are less expensive than their competition, but offer
comparable construction and design features. The model 5512 costs
about $1,000 less than the next larger Vetus unit. We could find
no competitive unit that would fit as well into the fore-and-aft space
available.
Power supply options were (1) operate the unit from the existing batteries
aft and run heavy cables to the thruster, and (2) provide a separate
battery for the thruster and install a charging arrangement to keep
it topped off. We decided to go the latter route owing to the size,
weight, and expense of no. 4/0 gauge cables and the difficulty of routing
them through the boat. Our design for the electrical system, diagrammed
on the attached page, was derived from the recommendations of the Yandina
Company (http://www.yandina.com/),
and we bought our battery combiners and circuit protection from them.
Cabling and connectors came from Northern Arizona Wind and Sun (http://www.windsun.com/).
I installed a group 27 “dual purpose marine battery” from
Sam’s Club; David went with a size 31 AGM battery to match the
rest of his batteries as to charging characteristics. Both of us secured
the batteries in home-built steel brackets attached to the bulkhead
aft of the water tank.
We
decided to control the thrusters with foot switches mounted in the floor
of the cockpit. Vetus sells hand switch controls and joysticks, but
we adapted their windlass control switches to the new task, requiring
that we make a minor modification to the control wiring harness. We
reasoned that (1) the helmsman already had enough work for his hands
in dealing with the steering wheel, shifter and throttle; and (2) that
installation of a conveniently located hand switch or joystick would
be a hassle on both our boats. The picture shows the floor of the cockpit
aft of the steering pedestal. The switches are shown with their protective
covers closed.
Installation
David
arranged with John Orm of Pelican Marine in
Tarpon
Springs, Florida
to do the fiberglass work; we had already decided to do the rest of
the project ourselves. John obtained the thrusters and tunnels, fuse
blocks, fuses, and switches directly from Vetus, and David and I accumulated
the remainder of the materials from the other sources noted above.
We did the electrical installations in advance, to minimize the expense
of our time out of the water.
Harmony was hauled on a Tuesday, and went back into the water
the following Friday after John had completed his work and repainted
her bottom. Twenty minutes after Harmony was launched, Meridian
went into the haulout slip. She was launched the following Tuesday
afternoon.

The photos show the installation in progress on Meridian. John
cut the holes in the hull using an electric reciprocating saw, and then
fitted, marked, and cut the tunnel tube. He then cut away the gelcoat
and several layers of laminate from an area around the hole on each
side using a laminate plane, and prepared the inside the hull in the
attachment area with a small electric grinder. After fitting and installing
the power head of the thruster to the tunnel on the workbench in his
shop (a departure from Vetus’ instructions but a major time saver),
he returned the tunnel to the hull, carefully aligned the centerlines,
and then “glued” it into place using polyester putty.
Once
the putty had set, immobilizing the tunnel, John applied several layers
of new fiberglass laminate to the inside of the hull. After the resin
“kicked”, he returned to the outside of the boat and laminated,
faired, smoothed, and painted the outside. Because of the extremely
close clearances on the inside of the boat, John was able to apply laminate
only to the top two thirds of the circumference of the tube. He added
the required strength in the exterior laminations by grinding away most
of the thickness in the bottom of the tunnel tube and building up the
laminate from there. The result maintains the tunnel’s inside
diameter while still providing adequate laminate thickness for strength.
After coating the new laminate, the bare tube, and the wetted parts
of the thruster with three coats of epoxy barrier, the bottom paint
was applied, completing the installation.

Note: Photo looks straight down on thruster compartment. Tunnel is visible
under the thruster motor. Wiring is hidden by berth platform. UP is
FORWARD.
The interior part of the installation was completed by painting the inside
of the compartment, including the new tube and fiberglass bonding, fitting
the drive motor and battery bracket, and hooking up the wiring. We tested
the operation of the unit and then prepared
Meridian to be launched.
John gave the tunnel a final check while we were afloat but still in the
slings.
When we got home we gave the new equipment its first real operational
test, and we were very pleased. We can turn Meridian 180 degrees in her own length using
engine reverse and thruster, then forward and thruster. There’s
no more anxiety about picking up the bow line on the first pass. If
it’s missed, we just move the bow toward it a bit, enabling another
try. Subsequent practice has confirmed the dramatic improvement in
control, and it certainly seems that we will make a lot of use of this
new labor (and anxiety) saving device.
Costs were $1,485 for the thruster unit, tunnel, battery, bracket,
and electrical cables and equipment, and $631 for installation materials
and labor, for a total of $2,116. The costs of hauling, launching,
and bottom paint are not included; Meridian was due for bottom
paint anyway.
Diagrams of the electrical installation and the homebuilt battery bracket
are on the following pages.
If other owners have questions about the details of this project, I’d
be glad to discuss it with them. My email address is Lee
Thurner.

Follow up in July, 2006
Pat Noordsij: Now that it has been 4 yrs, are you still happy with
the Vetus 5512?
David Kimmel: Every time I leave or enter the slip it puts a smile
on my face....
It would have been nice to have gotten a larger unit. However it would
have
requried a much larger amount of cash and redoing the V-berth. In this
case
it just used a small space that I never used that much to begin with
and the
cash outlay was a great ROI.
There are times when the wind and the current over power the thuster
because
of its smaller size. I am not even sure if the bigger units would be
that
much help in these case due to our windage.. These are the time we just
have
to go back to our boat handling skills..
There is nothing like being dead tired and easly backing into or pulling
into a difficult berth with no worries. Oh and I love being in a slip
that
is way too big and use the bowthruster to bring the bow to port or starb.
to
set the lines... Way easier ...
The best part is it has worked flawlessly for the past 4 years....
So yep still happy. Just wished I had done it sooner!!
David